TEPI VICO CAPILLARY STRING WORKSHOP
Sharing the experiences key success for the future !!
Quick overview: liquids loading phenomena in gas wells
new well,
high gas rate
Well died !!
At initial stage of production, the gas will
carry produced liquids up to surface as the gas
velocity is high enough.
The energy available to transport the
produced liquids to surface declines due to the
depletion drive of reservoirs.
When the gas produced are below gas
critical rate, the liquids start to
accumulate in the wellbore
increasing hydrostatic pressure, back
pressure into formation. As a result, the
gas rate will significantly drops and the
well died
Decreasing gas rate
Liquid loading issue will always occurs in gas wells, just only wait in the
matter of time when it comes !!
TEPI VICO Capillary String Workshop
Targeted wells; 2 types
1 2
GAS RATE
Offloads
23
IP of the well is downgraded because of partial water
loading
The well is able to produce during a long period
Offloads are less frequent
Water loading limits the gas rate
Objective of capillary = enhance the gas rate
1- 2
months
TIME
GAS RATE
Offloads
1 2
3
IP of the well is deceasing very fast after offload due to
water production from the reservoirs
Very fast transition (a few days) from steady state (offload)
to death
Frequent offloads between repressurization period
Water loading kills the well
Objective of capillary = stabilize the rate
TIME
1- 2 weeks
TEPI VICO Capillary String Workshop
Test the limit of foaming technology !!
Turner Velocity
50% above Turner
velocity line
validated in 2010
campaign
Below 50% Turner
velocity line
validated in 2011
campaign
Weak wells
loading mode
reps. pseudo died
category
need special
operating procedure
Conclusion: Foaming technology can be applied in all region BUT it will
not work if the well has reservoir pressure issue (some black wells)
TEPI VICO Capillary String Workshop
Some good results: Off-loaded wells, critical velocity <50% of the TURNER speed
Surfactant
60 L/D
Qg: 1.3 MM
Qw: 25 bwpd
TN-X8 was in
Regular offloadcategory
With CS
Sustainable production for 16 months
(No off-load was required)
Surfactant
60 L/D
Qg: 0.8 MM
Qw: 30 bwpd
TEPI VICO Capillary String Workshop
TN-H5 was in
Regular offload category
With CS
Sustainable production for 12 months
(No off-load was required)
The special one !! good surprise of revival
Long offload
+test
Long offload
+ test
Well
revival
Qg: 5.2 MM
TN-F7 was in died
category since 2010
~1 month
~1 month
With CS
Intermittent production = 7
MMscfD more than 4 weeks
Unique well (died, even only
shut in for 2 hours)
Very good response if the well has strong inflow (high DEQ) but severe problem in
the outflow
TEPI VICO Capillary String Workshop
The died well: negative response !!
TN-ML5 was in died category
Negative response (production
can not be sustained):
Offload 4x
1x intermittent well opening
Negative response due to reservoir pressure issue (low deq)
TEPI VICO Capillary String Workshop
TN-X8: Dewatering dP downhole evaluation
Production Evolution on Well TN-X8
5
100
90
80
60
QG increase After surfactant injection
50
40
30
20
10
SI for CS
installation
LP
mode
0
17-May-11
WHFP (Bar)
Surfactant Inejction rate (L/D)
Gas Rate (MMSCFD)
70
0
6-Jun-11
26-Jun-11
Gas Rate
Surfactant Injection Rate
16-Jul-11
5-Aug-11
Water Production
25-Aug-11
oil Production
14-Sep-11
WHFP
DP downhole linked to dewatering is > DP linked to LP mode
TEPI VICO Capillary String Workshop
DEPTH REACHED (TARGET VS ACTUAL)
Some tolerance to the setting depth
TEPI VICO Capillary String Workshop
Result of current FAL project (per W1 Dec 12)
No.
Well
Site
TN-T6
TN-X8
TN-H5
TN-H3
TN-F5
TN-F7
TN-R23
TN-K11
TN-P14
TN-P23
TN-H12
TN-I9
TN-Kx23
TN-TMx30
TN-Dx20
TN-M18
TN-I1
TN-F11
TN-Lx41
SPU
SPU
SPU
SPU
SPU
SPU
SPU
2
3
4
5
6
7
8
9
10
11
12
13
14
15
16
17
18
19
NPU
NPU
NPU
SPU
NPU
NPU
SPU
SPU
NPU
NPU
SPU
NPU
Phase
Date
2-Dec
2-Dec
2-Dec
Pilot
2-Dec
2-Dec
2-Dec
2-Dec
2-Dec
2-Dec
2-Dec
2-Dec
2-Dec
Industria 2-Dec
l
2-Dec
2-Dec
2-Dec
2-Dec
2-Dec
2-Dec
TOTAL
(12)Wells flowing
1.27 MMSCFD / Well flowing
SPU
NPU
Highlights from pilot phase
Pilot Phase
Indus. Phase
Gas Rate
0.54 MMSCFD
0.38 MMSCFD
0.82 MMSCFD
0.35 MMSCFD
0.00 MMSCFD
4.76 MMSCFD
0.00 MMSCFD
0.40 MMSCFD
1.79 MMSCFD
0.00 MMSCFD
0.00 MMSCFD
0.00 MMSCFD
0.25 MMSCFD
1.20 MMSCFD
0.00 MMSCFD
3.69 MMSCFD
0.00 MMSCFD
0.55 MMSCFD
0.52 MMSCFD
Surf. Inj.
Rate (L/D)
20
60
60
30
5
150
0
126
50
15
15
5
40
80
100
60
0
100
40
WHFP (bar)
WHFT
(deg C)
14.5
11
12
12
0
23
60
9
12
11
10.5
9.4
7.9
13
107
10
10
26
12
36
33
35
33
0
57
0
36.6
41.7
30
31
0
35
46
0
50
0
57
33
15.25 MMSCFD 956 L/D
in Network
Total
8.60 MMSCFD 500 L/D 620 L/D
6.65 MMSCFD 316 L/D 336 L/D
6.84 MMSCFD 325 L/D
8.41 MMSCFD 631 L/D
Gain obtained 6.84 MMscfd (5 wells put on production).
TN-F7 rePoP after offload (+4.8 MM) ; TN-F5 plugged due to drilling activity. TN-X8 still low after misunderstanding of program.
TN-R23 is SI due to need to replace a part of DH equipment.
Highlights from Industrial phase
Gain obtained 8.41 MMscfd (7 wells put on production).
TN-M18 rePoP : +3.7 MM
TN-I9 rePoP failed : inject de-mineral then stop injection while waiting rig move out.
TN-I1 is waiting rig move-out for an intervention (gas found in control line)
TN-P23 SI for pressure Build up
TN-Lx41 rePoP : +0.5MM
TN-H12 died after switch to MP. SIBU
TN-Dx20 to be rePoP this week.
7 wells are still shut in due to DHSV packing leaking, work over, plug due to rig activity and
pressure build up
TEPI VICO Capillary String Workshop
DESIGN FEATURES
To keep down-hole safety valve installation
To reach target injection depth (3000 ~ 5000 m)
To avoid gas through inside capillary string
To be able to inject 150 L/D whilst maintaining DHSV
open
TEPI VICO Capillary String Workshop
INSTALLATION PROCEDURE
DOWNHOLE EQUIPMENT SCHEMATIC
WIRELINE PREPARATION:
RIH Dummy CS Hanger
RIH Memory P/T Survey
CAPILLARY STRING:
RIH Capillary String with Bottom Injection
valve to target depth
Cut Capillary String at surface
WIRELINE/BRAIDED LINE:
Connect CS with Hanger
Deploy CS with Hanger using Braided line
Function test the CS Installation
TEPI VICO Capillary String Workshop
12
TEPI CAPILLARY STRING COMPLETION
INDUSTRIALIZATION PHASE
2.81 DHSV Inside CS
Hanger. Opening
pressure 2000 psi
Top Injection Valve
inside CS Hanger.
Crack pressure 3200
psi
3/8 CS
Max 4800 lbs
Bottom Injection
Valve
CRACK
CRACK
TOP
BOTTOM
INJECTION
INJECTION
VALVE AT
START
Pressure
OPEN up
DHSV
Control
AT 2000
line PSI
VALVE
3200
AT 4000
PSI PSI
CHALLENGES
Down-hole equipment reliability
To simplify installation process
Running use CS Unit & deploy still
utilizes Braided line
Reduce crane dependency
TEPI VICO Capillary String Workshop
Surfactant Injection Surface Facility
Overview and Design Basis
Well Location
- Scattered Location Around Tunu Area
- Instrument Gas is The Main Motive/Control Fluid
- Limited Electrical Power (in some area is not available at all)
Design Basis
- Injection Pressure : 159 332 Barg
- Injection Flowrate : 10 150 LPD
- Positive Displacement Pump (Pneumatic Driven) Selection Based on API-675
TEPI
15 VICO Capillary String Workshop
Surfactant Injection Surface Facility
Injection Package - Simplified Block Diagram
Safety Equipment
(Surfactant Injection
Isolation Valve)
TEPI
16 VICO Capillary String Workshop
Safety Equipment
(Pressure Protection)
Pump, Regulator
and Filter
Safety Equipment
(Instrument Gas Supply
Isolation Valve)
Surface facilities package
Surface facilities package will be
removable. Once the capillary
well is finished, the package will be
used for the other well
TEPI VICO Capillary String Workshop
17
Surfactant Injection Surface Facility
Challenges
Modification on Existing Infrastructure/Facilities
- Various Type of Structure and Configuration
- Portable Injection Facilities (Structure/Platform, Tank and Injection Package)
Surfactant Liquid Compatibility
- Corrosion Issues
- Instrument Seal vs Surfactant Liquid Compatibility
- Surfactant as Safety Valves (DHSV) Motive Fluid
Engineering and Design Condition
- Required Injection Pressure and Flowrate (Sensitive to Wells Characteristic)
- Instrument Gas Issues (Low Pressure, Condensation)
Alternative Solution : Gas Amplifier ?, Local Gas Scrubber ?, Electric Driven Pump (by
Solar Panel + Battery)?
TEPI
18 VICO Capillary String Workshop
Development of surfactant test bench
Sign of chemical
degradation
TEPI VICO Capillary String Workshop
Onsite
If chemical
degrade, end of
story !!
FOAMING & EMULSION ISSUE
REVERSE
DEMULSIFIER
INJECTION
DEFOAMER
INJECTION LINE
FLOTATOR
NMP3 SC
SAMPLING POINT
TO DISPOSAL
TUBE
TO FOST
SURFACTANT
INJECTION
450
12000
400
10433
10219
9910
9645
350
9259
380
10000
380
9426
8965
8939
330
300
8029
6334
260
6782
240
230
230
200
6000
5318
150
Produced Water (bbl/d)
8000
7013
250
Water Oil Content (ppm)
Surfactant Injection (L/d)
Defoamer Injection (L/d)
Produced Water (bbl/d)
4162
140
140
3386
100
3144
2922
32.9
50
7.8
8.2
8.3
8.7
7.9
7.1
7.3
7.8
7.2
40
8.6
8.1
7.8
7.9
9.3
9.1
20-Sep-12
21-Sep-12
22-Sep-12
23-Sep-12
24-Sep-12
25-Sep-12
26-Sep-12
27-Sep-12
28-Sep-12
29-Sep-12
30-Sep-12
1-Oct-12
2-Oct-12
3-Oct-12
4-Oct-12
5-Oct-12
19.6
7.9
17.2
2000
9.1
9.0
9-Oct-12
80
50
3190
10-Oct-12
80
4000
3243
2972
100
-50
TEPI VICO Capillary String Workshop
8-Oct-12
7-Oct-12
6-Oct-12
20
Conclusions & Way forward
The Capillary String project is profitable. The additional gas production is obtained and
can sustain/prolong the life of liquids loaded wells.
Foaming & emulsions issue shall be solved asap to maintain project delivery.
Continue learning process to get comprehensive understanding about capillary foaming
technology.
TEPI VICO Capillary String Workshop
21