Reduce Defect Accuracy IMV 5 Model by Eliminating Problem NTC
Stamping Part 67189-0K030 Reinforcement Back Door Stay
Name
: Reza Rahmaputra
Date Of Entry
: 02 September 2013
No.Reg
: 1324394
Department
: Vehicle Quality Prod. Engineering
Section
: Vehicle Quality and Planning
TMMIN VISION 2014
DIVISION KPI
To be the Best and the Most
Flexible in Asia Pasific
Zero Defect Outflow To
TMMIN
A. TMMIN PART CHAIN MAP
->
Project Management & Control
Toling Progress & Control
Tooling Technical Support
Quality & Accuracy Approval
Quality & Accuracy Achievement
->
No
Item
Accuracy
Target (%)
Confirmation
Vehicle (CV)
95
Soukaku (SKK)
2
3
Goshi (1W)
100
Accuracy Achievements Target
100
90
80
70
60
85 86
76
10-12
1-3
TOOLING KICK OFF
4-6
7-9
10-12
1-3
4-6
Goshi
Soukaku
7-9
Mass Product
Trial ( MPT)
10-12
Qty Defect
100
MPV
112
Rank
17
CV'Feb
Week IV' April Soukaku
59
0
Defect Surface Defect Accuracy
Defect Spot
Weld
16
(14 DA)
12
8
CV
Accuracy
(Trimline,Aspec
Surface, Hole
Position)
Part Surface
Rank
No Defect Outflow
Rank
Week IV'April Soukaku
Provide Good Quality, Good Process,
Achieve Production Volume & No Delay
Current Condition
By Where
Problem
59 DA at NTC
59 Defect Accuracy on
CV Activity (February
2014)
By Category Part
35 DA at
Stamping Part
By Part Number
18 DA at R/F Back door
Stay (67189-0K030)
Items
Qty Problem
Trimline
Aspec Surface
Hole Position
Appearance
Total
0 DA at Others
Supplier
Pareto Diagram
16
24 DA at Sub Assy
Part
10 DA at R/F Quarter wheel
House (61671-0K020)
7 DA at Hood S/A, Hood
Lock (53831-0K050)
12
18
10
0
61671-0K020
53831-0K050
13
18
67189-0K030 R/F Back Door Stay
Part
Trim Pierce 1
Dies NG
Gap
Fitting Panel
NG
Radius Panel x Radius
Dies Unmatch
Dies Process Trim
Pierce 1 Repaired
(Setting)
February
II
IV
PIC
March
II III IV
April
II III IV
Trimline Plus Ilustration
Act : Radius Panel < Radius Dies
Std : Radius Panel = Radius Dies
May
II III IV
AA
SURFACE
(-)
STD : 0.5
(+)
ACT : +0.8
Part
(-)
BA
June
II III IV
Schedule
July
II III IV
Aug
II III IV
: STD
: ACT
Lower
Dies
TRIMLINE PLUS
STD : 0.7
ACT : +1.5
Sept
II III IV
Oct
II III IV
Nov
II III IV
Dec
II III IV
Die Repair 3
Trial and Repair 2
Trial and Repair 3
Judgment
Soukaku
Activity
Judgment
Result and Feedback
No SOP For Panel
Fitting
Upper
Dies
STOPPER
PAD
Accuracy Achieved 96%
and SOP Implemented
Defect Accuracy Investigation
Die Repair 2
NTC Dies
Maintenance
(Baharudin),
VQPE (Reza)
: STD
: ACT
Lower
RC #2
Result
SOP Compiling and Approval
Implementation SOP
Make SOP For Fitting
Panel
VQPE
(Reza),NTC
(Budi)
Result and Feedback
. Aspec Surface Repair
Upper
Dies
Upper
Dies
*Defect Accuracy Related :
Upper
Dies
STOPPER
PAD
Lower Dies
LOWER
Panel Moved When
Trim Pierce 1
Process
Spec Material
Equal with
standard
Radius Panel x
Radius Dies
Unmatch
Countermeasure
. Trimline Minus Repair
Panel Not
Fitting
Machine
()
Defect Accuracy IMV 5 Model 59 DA on CV
Activity (February 2014)
Panel Moved
(+)
( and )
Defect Accuracy IMV 5 Model 59 DA on CV Activity
(February 2014)
Trimline Minus Ilustration (, and )
Panel not Fitting Ilustration ()
Material
Inefficiently
Fitting Panel
Root Cause
Rank
GAP
STEP 2 BREAKDOWN THE PROBLEM
1W
DIES
MP
Experience
Level 3
* DA = Defect Accuracy
Defect Accuracy IMV 5 Model 0 DA on CV Activity
(February 2014)
Ultimate Goal
STEP 5 DEVELOP COUNTERMEASURE AND COUNTERMEASURE
Spot
Weld
Burry,Marking,Kaji
ri and Emboss
R Panel < R Dies
Notes :
MP : Man Power
SOP : Standard of Procedure
NG : Not Good
RC : Root Cause
STEP 4
Reduce 14 DA and
Accuracy Achievement 95%
From NTC Stamping Part
Reinforcement Back Door
Stay (67189-0K030) in
Trim Pierce 1 process until
week IV April 2014
Defect Decrease Target
18
20
RC #1
Ideal Condition
STEP 1 CLARIFY THE PROBLEM
Defect Accuracy
Problem Founded
1W
No SOP For
Panel Fitting
STEP 3
STEP 2
Check by
Proto and
Designer
Key Point :
Methods
Form Ability
(Crack,
Shiwa and
Nobi)
Proto Check
Check by
Inspector
Cam Pierce
Man
CV FEEDBACK AND REPAIR
STEP 1
Rank
67189-0K030
Flange
18 Defect Accuracy From NTC Stamping
Part Reinforcement Back Door Stay
(67189-0K030) in Trim Pierce 1 Process
All Accuracy CV Part
Achieve by TMC Proto
with Feedback : Need
level Up and No
Handwork For Soukaku
(SKK) Activity.
F. STEP HOW TO REPAIR
Rank
y7
Cam Pierce
Actual
2015
CONFIRMATION
VEHICLE (CV)
E. CV PREPARATION PROBLEM FOUNDED
Inspection
Process
Target
2. Soukaku (SKK) is Trial Confirmation activity both press part and weld tooling.
Reza R.Putra
100
95
95
1. CV Preparation : All CV Part From Supplier Checked Quality and Accuracy Achievement by TMC Proto
20
Muh.Anhar K
STEP 3 SETTING TARGET
85
*Notes :
50
Trim Pierce
1
Forming
Before CV
2014
CV PREPARATION
150
Ndaru J
STEP 4 ROOTCAUSE ANALYSIS
7-9
FMC
Nicholas A
Cutting
Cutting
Lower
Dies
Lower
Dies
STANDARD OPERATION PROCEDURE (SOP)
NO : SOP-DB00-2301
PROCESS
PANEL FITTING
TANGGAL
: 30-04-2014
REVISI
: 0 KE
HALAMAN
: 1 dari 1
NO FAKTOR
Cutting
Cutting
Add
Weld
Add
Weld
. Making Procedure For
Fitting Part
Add
AddWeld
Weld
M
Q
Q
M
Q
Q
Q
Q
M
M
Q
Q
Q
Q
Q
Q
Q
Q
Q
Q
Q
Q
Q
Q
LANGKAH KERJA
1.0 Ambil panel buat panel fitting
1.1 Taruh panel diatas die yang akan di panel fitting
1.2 Beri tanda pada panel dengan spidol cat
1.3 Bawa panel ke lokasi mesin plasma
1.4 Lobangi panel yang diberi tanda dengan spidol cat
1.5 Bawa panel dekat dienya yang mau di panel fitting
1.6 Ambil gerinda pada tempatnya
1.7 Rapikan hasil plasma dengan gerinda
1.8 Kembalikan gerinda pada tempatnya
1.9 Bersihkan panel dari kotoran
2.1 Ambil akaipaint dan kwas pada tempatnya
2.2 Oleskan panel bagian yang penting dengan akaipaint
2.3 Kembalikan akaipaint dan kwas pada tempatnya
2.4 Ambil tanah liat pada tempatnya
2.5 Perhatikan bagian yang penting
2.6 Taruh panel diatas die yang akan di panel fitting
2.7 Ketok panel dengan tangan atau tangkai kwas
2.8 Angkat panel
2.9 Panel taruh tempat yang aman
2.9a Ulangi step kerja no:1.9 hingga 2.9
2.9b Hingga bagian penting atarinya benar-benar rata
2.9c Gosok bagian atari
2.9d Sanding bagian-bagian yang kurang penting
2.9e Die selesai proses panel fitting
DEPT
SECT.
LINE
DISAHKAN
: TM
: DAT
: T/O
DIPERIKSA
DEPT. HEAD SECT. HEAD
HAL PENTING (KEY POINT)
-Ambil panel proses sebelumnya
-Perhatikan model panel terhadap Lwr die
-Tandai bagian panel yang bersentuhan
-Gunakan Dolly
-Gunakan mesin plasma untuk melobangi
-Gunakan Dolly dan taruh tempat yg aman
-Gunakan gerinda sesuai kebutuhan
-Panel sebelum di panel fitting harus rapi
-Taruh gerinda pada tempatnya
-Gunakan majun hingga bersih
-Campuran Akaipaint harus rata
-Oleskan panel yang bersentuhan dng model die
Taruh Akaipaint Pada tempatnya
-Tanah liat warna merah
-Beri tanah liat sedilit bagian yg penting/ kijun
-Panel jangan sampai rusak / penyok
-Ketok panel secara pelan pelan
-Angkat panel berdua apabila panel ukuran besar
-Gunakan cover
-Ulangi step kerja1.9 s/d 2.9
- Atarinya rata dan panel tidak labil/goyang
-Gunakan batu gosok #80,#120
-Gunakan gerinda sanding
Die siap Pad Awase
DIBUAT
LINE HEAD
ILUSTRASI
1
Part Forming
yang OK
: OK : NG
Point Check
OK
59
Defect Decrease Result
18
20
15
10
3
5
0
96
100
86
90
76.6
80
70
Before CV
CV'Feb Week IV'April
CV'Feb
Week IV'April
* Contributed to the Gap Condition : (15/59)*100%= 26% Reducing Defect
STEP 6 MONITORING RESULT
Before Repair
Accuracy Achievement
Accuracy (%)
IMV 5
Nandy J
Problem to Tackle:
18 Defect Accuracy from NTC Stamping Part Reinforcement Back Door Stay (67189-0K030) in Trim Pierce 1 Process
: Main
: Support
2013
LEVEL
Prepared by
Point of Occurence
D. PROJECT MILESTONE
MODEL
Checked by
C. QUALITY PERFORMANCE INDEX
TMMIN
Supplier
PUD VQPE
ITEM
Supplier
"0" Defect Outflow
B. PRODUCTION ENGINEERING ROLE
TMMIN
JOB RESPONSIBILITY
Part Accuracy and Quality
Management
Approved by
Stamping Process
Blanking
DEPT. KPI
Acknowledge
Case (Defect)
Division
: Prod.Eng Division
BACKGROUND
Flow Process:
Acknowledge
Case (Defect)
PT. TOYOTA MOTOR MANUFACTURING INDONESIA
PRODUCTION ENGINEERING DIVISION
VEHICLE QUALITY PRODUCTION ENGINEERING DEPT.
NG
18
Total : 77
Accuracy
76%
After Repair
: OK : NG
Point Check STEP 7 STANDARDIZATION
OK
74
NG
3
Total : 77
Accuracy
96%
No Handwork ( Full
Dies Output)
5W1H
Item
WHY
Panel Fitting No Mistake when
Procedure
fitting part
WHAT
WHEN
WHERE
WHO
HOW
SOP
Try out Activity
NTC Plant
Operator
Fitting Part
Confirmation
STEP 8 NEXT ACTION
>Follow Up Level Up Activity 67189-0K030 Until Soukaku Activity
>Reduce Defect Accuracy at Reinforcement Quarter Wheel House
0K020)
(61671-