Manufacturing of Piston: Mechanical Engineering
Manufacturing of Piston: Mechanical Engineering
ON
MANUFACTURING OF PISTON
Submitted in partial fulfillment of the requirements for the award of
Bachelor of Technology
In
MECHANICAL ENGINEERING
BY
Mr.ARVIND YADAV
Assistant professor
CERTIFICATE
This is to certify that the Industry Oriented Mini project work entitled
“MANUFACTURING OF PISTON” is a benefited record of the work done by
This record has not been submitted to any other University / Institution for the award of any
degree/diploma.
Mr. K Sheshacharyulu.
EXTERNAL EXAMINER
ACKNOWLEDGEMENT
A project work of this magnitude is not possible without the help of several people
directly or indirectly. It is with immense satisfaction that we present our practical experience in
the form of project report on “MANUFACTURING OF PISTON”
We wish to express our sincere thanks to Prof.RAM PRASAD, Principal, DVR College
of engineering and technology, for his constant encouragement in doing this project.
I would like to thank my guide. Mr.ARVIND YADAV for taking keen interest in my
training and giving me a chance to carry out this project under his supervision and also for
providing all the required technical knowledge and support required for this project.
I would also like to thank all the members of production department of SAMKRG
PISTONS AND RINGS PVT Ltd. for giving me a helping hand in the course of this project.
We extend our thanks to our entire faculty of mechanical engineering department and all
those who have been directly and indirectly involved during the tenure of our project work.
A tool after finishing of 5000 number parts production “white band’’ problem is
identified on outer diameter piston with “ NATURAL DIAMOND TOOL’’ Many of parameter
are to be considered like speed, feed, depth of cut, tool and work piece alignment, tool geometric
parameters etc. Even though using CNC work station the problem is repeated in a particular
model with natural diamond tool. Although certain parameters like tool speed, feed, and depth of
tool / work piece alignment are computer numeric controlled (CNC) still the problem band is
repeated with poor surface finish. So, we concluded that the geometry of tool has to be analyzed
against roughness variation. We made certain no. of calculations on roughness (Rt) by changing
rake angle , cutting angles (Ce,Cs) found good surface finish on piston OD surface without
White band and also improve the tool life.
INDEX
CONTENTS
CHAPTER 1
1.0 INTRODUCTION 1
CHAPTER 2
2.7.4 DEGASSING 15
2.8 CASTING 17
2.8.1 STEPS INVOLVEDD IN CASTING PROCESS 17
CHAPTER 3
3.6 INSPECTION 41
3.6.1 DIMENSIONAL INSPECTION 41
CHAPTER 4
4.0 CONCLUSION 43
CHAPTER 5
5.0 BIBLOGRAPHY 44