SPE-203603-MS Lessons Learned From Drilling A Long Open Hole Interval and Recovery From A Stuck Pipe Incident
SPE-203603-MS Lessons Learned From Drilling A Long Open Hole Interval and Recovery From A Stuck Pipe Incident
Lessons Learned from Drilling a Long Open Hole Interval and Recovery
from a Stuck Pipe Incident
Ayodele Akinfolarin, Obinna Amah, Isijokelu Ijeh, Chiwar Djauro, Samson Omoregie, Mike Usim, Willhelm Tien,
John Emesi, and Joseph Mordi, The Shell Petroleum Development Company Nigeria Limited
This paper was prepared for presentation at the Nigeria Annual International Conference and Exhibition originally scheduled to be held in Victoria Island, Lagos, Nigeria,
11 - 13 August 2020. Due to COVID-19 the physical event was not held. The official proceedings were published online on 11 August 2020.
This paper was selected and peer reviewed for presentation by an SPE program committee following review of information contained in an abstract and paper submitted
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Abstract
Drilling long open hole sections has been known to result in many challenges including wellbore instability
problems which may lead to stuck pipe problems. However, well design or operational challenges may
necessitate making such risky decisions. In such situations, precautionary measures will need to be taken
to ensure that the hole is successfully drilledwith minimum to no wellbore instability problems which have
negative impact on time and cost.
The case study, well FX-3 is a well drilled by one of the major oil and gas companies in the Niger Delta.
The tophole was planned to be drilled in two sections: a pilot hole to the planned section total depth and then
with a hole opener to open the pilot hole to the required hole size. Due to the abrasive formation type and
difficulties encountered while drilling to the planned depth, decision was made to set the casing shallower
than planned. This necessitated drilling the 12-1/4" hole section longer than planned. With this decision,
several challenges were encountered and eventually overcome. The well was successfully completed.
The objective of this paper is to present the lessons learned in drilling a long open hole interval and the
recovery operations from a stuck pipe incident within that interval in the well. It discusses both the well
design and actual field practices, with significant emphasis in the recovery operations from the stuck pipe
incident. One of the key events is the spotting of special pipe freeing pills, which in combination of other
activities led to the freeing of the stuck bottom hole assembly which had a radioactive source. Some of the
key learnings are the need to optimise the well design, proper hole cleaning and mud conditioning prior
to drilling to section total depth. The knowledge of the pipe sticking mechanism and the application of the
right pipe freeing formulations are important considerations in freeing any stuck pipe
Introduction
Drilling long open hole sections could lead to many borehole stability problems such as improper hole
cleaning, stuck pipe or hole collapse. In some cases, long open hole intervals that travess different formations
(such as a combination of depleted intervals with high pressure intervals) may also lead to loss of drilling
mud to the formation, consequently resulting in loss of hydrostatic head and potential well control problems
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in extreme cases (Warlick, 2009; Hassan, 2018). With stuck pipe taking up a huge part of drilling costs
(Bradley, 1991), various approaches have been designed to prevent and also recover from its occurrence,
including the use of pipe freeing pills (Aadnoy, 1999; Krol, 1981).
Well FX-3 is a development well that lies somewhere in the coastal waters in the Niger Delta. The well
is located on a platform on the shallow waters off the coast of the Niger Delta. The well was drilled with
a Jack-up rig. The initial design of well FX-3 involved the drilling of about 6300ftah of open hole in the
12 ¼" section after drilling and securing the 16" hole with 13 3/8" casing. This design was predicated
on the isolation of freshwater aquifer and the installation of a blow-out preventer before penetrating the
shallowest hydrocarbon. It was also required to set the production casing deep enough to acquire sufficient
shoe strength both for well control and equivalent circulating density considerations and to minimise the 8
½" hole interval. The overall casing design concept of well FX-3 is presented in Figure 1 below. The well
plan showing the well deviation is also presented below (Figure 2).
This paper presents the drilling of some sections of Well FX-3 and the recovery operation from a stuck
incident in the 12 ¼" hole.
pull and 100 klbs slack off weight with 300gpm circulating rate. However, the casing was successfully run
to setting depth of 4045ftah and cemented in place.
An investigation into the reasons the two-hole opener BHAs could not open the 8 ½" pilot to the planned
section total depth indicated that the formation was abrasive as the five bits deployed within this interval all
came out under gauge. The investigation also showed that the hole openers could have been made of PDC
or TCI cutters or milled tooth cutters of higher IADC classification.
down the filter cake. An analysis of the freeing mechanism the second time the string was free indicated
help from two likely sources. First, the caustic pill may have broken down the filter cake across the stuck
interval. Second, the axial force due to the parting of the string may have led to some severe shock load
(combined slacking of the weight of the entire string with some impulse force) on the stuck interval, leading
to the freeing of the stuck string and allowing it to fall to bottom.
Figure 4—Part of the string that parted on surface. The lower part of the fish was in hole at the time of this picture.
After the pipe was pulled to surface, a decision was taken to immediately run the 9-5/8" production casing
since extensive back-reaming operation was done while pulling the stuck string to surface. The casing was
run without much issues through all the intervals that were back-reamed up to 11049ftah where it was held
up. That depth interval, 11049ft to 11200ft, was not back-reamed. The casing tally was adjusted, the casing
pulled to 11016ft and the casing hanger landed. The casing was cemented successfully. Worthy of note while
displacing the cement was that the plugs where not bumped after displacing the calculated displacement
volume. Additional volume of about 6bbls was pumped to bump the plugs. The additional volume was
calculated from the mud compressibility correlations. Subsequently, the well was drilled to the final target
depth and other well operations were conducted successfully.
Lessons Learned from drilling a long open hole interval and retrieval of a
stuck pipe
The following were some of the lessons learned in drilling a long open hole interval and retrieval of a stuck
BHA:
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i. 8 ½" hole can be opened directly to 16" hole. The Cutters of the hole openers should be selected
based on the formation to be drilled. Review offset data if available
ii. Consider the possibility of short wiper trip runs when drilling a long open hole interval
iii. Condition mud properties to the required specification while drilling (across depleted intervals) and
prior to pulling out of hole the bottom hole assembly
iv. Check that the HPHT filtrate loss is within the programmed value and the filtrate is all oil without
water indent prior to pulling out of hole the drill string.
v. Circulate the well clean till there are no significant returns of formation cuttings from the shakers
vi. Consider running casing rather than a wiper trip when the open hole interval has been back-reamed
at drilling or close to drilling parameters
vii. In highly deviated wells, it is possible for the drill string to be stuck mechanically and have full
returns if the cuttings bed is lying on the low side and not causing substantial obstruction to the
drilling fluid flow path. Mechanical sticking can be prevented by conditioning the drilling fluid
rheology to the right specifications and circulating the well free of cuttings
viii. Have enough quantities of caustic soda and pipe lax on location when drilling across intervals with
high risks of differential sticking
ix. Have acid (e.g. 15% HCl) on location when drilling across depleted intervals with a CaCO3 weighted
mud
x. The caustic pill was effective in freeing the pipe from the filter cake
xi. Consider pumping a long column of base oil across stuck intervals or above as may be required to
reduce the hydrostatic across the stuck interval while taking well control and other borehole stability
issues into consideration
xii. Once a decision is made to back-ream, consider back-reaming the entire open hole and circulate the
well clean at the previous casing shoe
xiii. Back reaming should be done at close to drilling parameters with control over the rotary overpull
to minimise the risk of twist off if restriction is encountered
Conclusion
The 8 ½" top hole section of well FX-3 was opened directly from 8 ½" to 16" and the stuck 12 ¼" bottom
hole assembly was successfully recovered. The 9 5/8" casing was run and cemented in place without any
significant issue. Cutter selection based on formation lithology should be taken into consideration in the 8
½" × 16" hole opener design. About 7151ft of 12 ¼" open hole was drilled successfully in one bit run without
any equipment downtime. Hole cleaning and mud conditioning to the required specification should be taken
into consideration in drilling a long open hole interval, especially if depleted intervals are to be penetrated.
The deployment of caustic pill formulation was effective in freeing the stuck BHA. The additional lesson
learnt was that the 9 5/8" casing was deployed close to setting depth after backreaming the open hole interval
without much borehole related issues.
Acknowledgement
The authors wish to thank all those that participated in the successful drilling of the surface and intermediate
hole sections of well FX-3 especially van Zwol Cee, Princewill Ekeadah and Grace Nnorom. The drilling
contractor personnel, the service company personnel, the company supervisors at both the well site and
onshore were some of the people that participated in the successful drilling of the more than 7000ft of
open hole and the retrieval of the stuck bottom hole assembly. We also wish to thank the Shell Petroleum
Development Company of Nigeria for giving us the permission to publish this work
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