QCC GRESSMEN (Magnesium)
QCC GRESSMEN (Magnesium)
Die
Didirikan : 09 September 1997
Kapasitas : 120 ton/bulan
r
Supriyanto
Irfan B
Sulisdiyanto
Ekwan
M. Teguh T Theme Leader A. Basith M. Fadil
Circle Leader
Team Leader
- Juara 2 QCC TAM-TMMIN
- Juara 2 QCC Directorat
Team Member
- Juara 1 Skill Contest TMMIN
- Juara 1 Skill Contest Thailand
Achievement : Achievement;
Target: Juara 1 Konvensi Directorat 2021
Juara 7 Konvensi TAM-TMMIN 2019 Not Konvensi
X : 2,8 X : 3,0 X : 3,0 X : 3,3 X : 3,2 X : 3,4
Y : 2,9 Y : 3,1 Y : 3,1 Y : 3,5 Y : 3,4 Y : 3,6
X : 3,2
Y : 3,4 X = 3,2
X =3,0
Y =3,1 Y = 3,4
Zone C Zone B
COVID-19
ZONE
NAME
Meeting
Solving
7NTools
Komunikasi
work
4s & Safety
8 Step
Leadership
Status
Multi Skill
7 Tool
Metting
Motivasi
Team
Kaizen
Target
Supriyanto
work
X Y X : 3,4
Team
Step
SUWANTO 5,0 5,0 5,0 5,0 5,0 5,0 5,0 5,0 5,0 5,0 5,0 5,0 A Y : 3,6
TEGUH 4,0 4,0 4,0 5,0 4,0 4,2 4,0 4,0 5,0 4,0 5,0 4,4 A
BASITH 3,0 3,0 3,0 4,0 4,0 3,4 3,0 3,0 3,0 4,0 4,0 3,4 B
SULIS 2,0 3,0 3,0 3,0 3,0 2,8 3,0 2,0 4,0 3,0 4,0 3,2 C Current
Fadil EKWAN P 2,0 3,0 3,0 3,0 3,0 2,8 3,0 2,0 3,0 3,0 4,0 3,0 C
X : 3,2
1 Y : 3,4
IRFAN B 1
1,0 2,0 1,0 2,0 2,0 1,6 1,0 1,0 2,0 3,0 2,0 1,8 D
FADIL 1
1,0 2,0 1
1,0 2,0 2,0 1,6 1,0 1,0 2,0 3,0 2,0 1,8 D
Sumbu Y
Covid -19
Enjoying
Bersahabat
Smart Training
menyenangkan
Inovasi training
Guide Training
PENINGKATAN SUCCESS
CHECK PELATIHAN SKILL MOTIVASI & KOMUNIKASI
Assessment Development Result
G-QCC 7 Tool
Waktu Training
dilakukan selepas
kerja normal
Foto sedang
training)
Menghilangkan
Urgensi Durasi Dampak Performa Point
Cost
thema thema problem kerja
15 NG Komposisi
Menghilangkan 1. Urgent 1. 12 Bulan 1. Defect 1. 100 juta 1. 25 %
1 NG Komposisi 2. Sedang 2. 9 Bulan 2.Complaint 2. 50 Juta 2. 50 %
Pouring 3. Sangat Urgent 3. 6 bulan 3. Reject 3. 10 juta 3. 100%
ProsesTerjadinya Problem
M/C Analyzer M/C Spectro
Replay No Replay
Buang
S afety Operator
Terkena
pecahan Die
Die Retak/Pecah
C ost
• Jika ada kesalahan komposisi kimia yang
berlanjut ke produk finish maka akan berdampak
serius terhadap benda kerja
Die retak/pecah
PRIORITY THEME :
PDCA
Eng Suranto Haddy P
A.1. Countinue Safety Daily Management A.1.1. Implementation PMRs Safety by SGA board 80% 100% Eng Suranto Haddy P
CASTING : DIVISION A.1.2. Comply SMK3 Gold 100% Gold 100% PDCA Eng Suranto Haddy
I.Nyoman W. P Masui Kubota
Tagor JD
(Claim customer)
Forkliftless A.2.2. Eliminate work at high place Zero Zero M/T A.Kohar Toto W.
3000 I. Reduction
Inhouse Competitiveness
2121 Implementation
1 A SAFETY A.1 Work Accident
TOYOTA MOTOR MANUFACTURING INDONESIA Zero Accident Zero Accident Eng Suranto Haddy P Director SMEC Division
2000 1617 PDCA
A.1. Countinue Safety Daily Management A.1.1. Implementation PMRs Safety by SGA board 80% 100% Eng Suranto Haddy P
DIVISION ACTION PLAN FY 2021/2022
M2
1202 1174
818 A.1.2. Comply SMK3 Gold 100% Gold 100% PDCA Eng Suranto Haddy P
1000
Prepare Audit
A.1.2. Rank Down Actifity 1 / Month 1 / Month Eng Suranto Haddy P
CASTING : DIVISION
Tagor J.D
Tagor JD
0 I.Nyoman W. Masui Kubota
FY17
FY16 FY18
FY17 FY19
FY18 FY20
FY19 BM Juganda S.
Prepare SVP
KPI FY 2020/2021 Resources
A.3. Reduce work difficulties (yarinikui shigoto) ownership by developNo.
A.2. Strengthen comfort workplace
A.2.1. Forkliftless
Company Activity
Hoshin at Casting Factory
Target 1202 m2 562 m2 Prepare Prepare Prepare
Eng Suranto Haddy P Dept.
Division Action in Manpower Budget
Juganda S
M2
8 1202 I. Inhouse Competitiveness
1174
6 6 6 6 1000 818 Implementation
6 1 A SAFETY A.1 Work Accident
Prepare
Zero Accident
SVP
Zero Accident Eng Suranto Haddy P
A.2.3. improve achievement of efficiency A.1.1.PEFF 0,92 PMRsPEFF 1,0by SGA board M/T
100% A.Kohar Toto W. PDCA
Rank
4 4 A.1. Countinue Safety Daily Management
0
Implementation Safety 80% Eng Suranto Haddy P
6
Rank
4 4 2000 1617
6
M2
2 4 4 1202 1174
B.2. Water Efficiency 2 1000 818
0 Prepare Implementation
Water FY17
FY16 B.2.1.
FY17 Reduce
FY18 FY18
FY19 water consumption
FY19
FY20 BM of production prosess N/A 0,0444 m3/unit M/T A.Kohar Toto W.
0,15 0,139 0,128 0,13 0
0,121 0,114 FY17 FY18 FY19 FY20
Eng Suranto Hariansyah
FY16 FY17 FY18 FY19 BM
(m3/unit)
0,10 B ENVIRONMENT
A.3. B.1.1.
ReduceReduce
work difficulties (yarinikui shigoto) Mapping
B.1. Energy Efficiency Running Equipment after Production off N/A Reduce 30% Implementation M/T A.Kohar Toto W.
0,05
Remain Rank at Casting
Rank
8,62 0,114 4 4
6
(m3/unit)
8,39 8,40,10
(Ton/unit)
8,5 8,17 2 4 4
0,05 2
8,0 0
FY17
FY16 FY17
FY18 FY18
FY19 FY19
FY20 BM
0,00
7,5 FY19 Eng Suranto Hariansyah
FY 16
FY17 FY18
FY 17 FY19
FY 18 FY20
FY 19 BM FY 16 FY18
FY17 FY 17 FY FY20
18 FY 19 BM
B.3. Waste Reduction B ENVIRONMENT
Prepare Mapping
B.1. B.3.1.
EnergyWaste
Efficiency B.1.1. Reduce Running Equipment after Production off N/A Implementation
Reduce 30% Implementation M/T A.Kohar Toto W.
B.4. CO2 reduction 8,86
Waste Reduction : N/A Reduce 5 % M/T A.Kohar Toto W.
9,0 Prepare Implementation
CO2 B.4.1.
8,62 CO2 reduction
8,39
Energy
8,4
saving through reduce unnecessary process (non Production) 0.053 Ton / Unit 0.048 Ton / Unit M/T A.Kohar Toto W.
(Ton/unit)
0,134 0,133 8,5 8,17
0,132
(Ton/unit)
0,132 0,131 8,0 B.2. Water Efficiency
Prepare
Suranto
Implementation
0,13 0,13
7,5 Water B.2.1. Reduce water consumption of production prosess N/A 0,0444 m3/unit M/T A.Kohar Toto W.
0,130 FY 16
FY17 FY18
FY 17 FY19
FY 18 FY20
FY 19 BM 0,15 0,139 0,128 0,13
0,121 0,114
0,128
(m3/unit)
0,10
FY17
FY 16 FY18
FY 17 FY19
FY 18 B.4.
FY20
FY 19 CO2
BM reduction
(Ton/unit)
0,132
2.1. Zero Out Flow & Claim Customer 2.1.1. Review
0,131 (Outflow) Zero Outflow Zero Outflow Eng Suranto Rio K.
0,13 0,13 B.3. Waste Reduction
0,130 Prepare
2.1.2 Eliminate reject die casting (No Re-Casting)
Waste ZeroReduction
B.3.1. Waste Re-casting
: Zero Re-casting SimulationN/A Eng 5 Suranto
Reduce % Rio K. Implementation
M/T A.Kohar Toto W.
9,0 8,86 Trial &
2.2. Increase Quality Achievement Continous 0,128
Improvement 2.2.1.
Next Process Defect 8,62Reduction by: Defect Next process : Process Die design
FY19 FY20 FY17 FY18 Evaluation
FY 18 FY 19 BM FY 16 FY 17 8,39 8,4 Study
(Ton/unit)
Defect Next Process 8,5
6,23919564
2.2.1.1 Achieve uniform solidification by gating system 8,17 Eng
Kick off Quality Suranto Rio K.
4,760291302 1TR QUALITY
2TR Cams 0,50% 0,40% Build In Quality Board
8,0
6,0
2
1,96164966 6 2,94720717 design improvement 8,0 Socialization Visualization
Campaign
PDCA
0,980535631,71047572 3,26
0,97165511 2.1.
1,5 Zero
0,67Out Flow & Claim
2.2.1.2 Customer 2.1.1.
7,5 Review buildby in quality in each process (Outflow) Zero Outflow Portable burner
Zeroinstallation
Outflow Eng Suranto Rio K.
4,0 8 5 Furnace RCS improvement
%
3,297010331,006540220,64907711 Eliminate excess gas source while pouring Eng Suranto Rio K.
2,0 6 8 1,32647494 1,54
8 7
2,04327535 4
7 0,4
0,5
0,6 1,05 FY 16 FY
FY17 FY18 FY19
17 FY FY20
18 FY 19 BM
0,0 3
FY17
FY16 FY18
FY17 FY19
FY18 FY20
FY19 BM 2.1.2 Eliminate
keep pouring temperature at last flasksreject
and die casting (No Re-Casting) Zero Re-casting Zero Re-casting Simulation Eng Suranto Rio K.
Trial &
Defect In Process 2.2. Increase Quality Achievement improve furnaceB.4.
RCSCO2
2.2.1. reduction
condition
Continous Improvement Next Process Defect Reduction by: Defect Next process : Process Die design Evaluation
6,63676994 Study Prepare Implementation
1TR 2TR Cams Defect Next Process CO2 B.4.1. CO2 reduction
Energy saving through reduce unnecessary process (non Production) 0.053 Ton / Unit 0.048 Ton / Unit M/T A.Kohar Toto W.
0,1342.2.1.1 Achieve uniform solidification by gating system Eng Suranto Rio K.
8,0 4
6,23919564 0,133 0,50% 0,40%
6,0 4,405493531,98558924 4,76029130 1TR 2TR Cams
4,0 4,717136582,74912631 8,0 2 2,94720717 2.2.2. Continous Improvement In Process Defectdesign
Reduction by:
0,132 improvement Defect In process :
%
5 1,3 6,02,03
1,96164966 6
(Ton/unit)
2,0 0,97617254
0,943460810,98005933
1
0,67630788
0,94381615
0,59577735
0,44599573 0,5
0,980535631,71047572
4,00,71 8 5 3,26 0,132 0,131 Tuning mixing process Improve squeeze
Portable & jolt
burner process
installation Furnace RCS improvement
%
3 6 7 5 2,03
M. Mujiono
80% 0.91 0.912 0.91 4,0 4,717136582,74912631 2.2.2. Continous Improvement In Process Defect99,00%
Reduction by: Defect In process :
%
2,03
3.1.1.3.
2,0 0,97617254 Rate
0,943460810,98005933
1 of 5Quality1,3
0,94381615
0,59577735
0,67630788
0,44599573 0,71
99,00% M/T
Tuning mixing process
A.Kohar Toto W.
Improve squeeze & jolt process
Ave FY16FY17FY17 FY18FY18 FY19FY19 BM
FY20 0,0 7 5 9 0,5
0,4
0,4 0,74
0,58 2.2.2.1 Improve mold quality by achieve optimum mold Eng Suranto Rio K.
7 4 1
4
90% FY17
FY16 FY18
FY17 FY19
FY18 FY20
FY19 BM 0,55% 0,41%
29,5668246 hardness and best water addition vsBenchmark
CB ratio Sosialization Implementation
3.2. Slim PEFF Casting 3.2.1. Smooth Implementation Casting PEFF
30,0 11,6021680
Repair
4
PEFF 0,986 PEFF 1,0 Prod Suranto Saripudin
1TR
9,230485417,50129985 2TR 15,1
1,1 1,05 3.2.2. Reduce Temachi through SW Kaizen4 N/A Temachi Max 3% Theme 1 Theme 2 Theme 3 Theme 4 Prod Suranto Saripudin
3.2. Slim PEFF Casting 3.2.1. Smooth Implementation Casting PEFF PEFF 0,986 PEFF 1,0 Benchmark
Trainning
Sosialization
Implementation at Casting
Implementation
Prod Suranto Saripudin
0,5 3.2.5. Create Master 3 TPS at Casting
PRODUCTIVITY N/A 1MP Prod Suranto Roni B.
1,1 1,1 1,05 3.2.2. Reduce Temachi through SW Kaizen N/A Temachi Max 3% Theme 1 Theme 2 Theme 3 Theme 4 Prod Suranto Saripudin
Step 0-2:Rencana Activitas
SCHEDULE ACTIVITAS CL DAN QCC GRESSMEN 2020/2021
YEAR 2020/2021
No. ACTIVITY PIC
Apr Mei Jun Jul Agust Sept
1 JUDGEMENT ASSESSMENT GROUP (CHECK) CL
4
Activitas QCC :
UPDATE SKILL (MONITORING) CL
THEME ACTIVITY
STEP 0-1 1. 14 Pertemuan meeting
PEMILIHAN THEMA Irfan
Fadil
= PLAN = ACTUAL
Step1 : Klarifikasi Masalah
NG
KPI Grafik NG Komposisi
Komposisi
GAP Pareto NG Komposisi Pouring
Pouring Berdasarkan Jenis Material Molten metal
Q Jan-Mar 21
12
Pouring Actual :
14
14
100%
100
14
95%
71%
10 N : 14 Kasus Sect. Head 80
8 Kasus M. Mujiono 11 Nn =
=1.41
14
Std : 0 Kasus
5 6 10 60
6
4 3 14 9
Material 40
0 1
Ideal : 0 D/U
0 0
9
60%
N = 10
80
70
5
6 84% 80
n = 1.41
NG Komposisi Pouring
Pada Material FCD
60
N=6 60
7
6 n = 0.91 50
4
Ketika Magnesium
40 40
5 Magnesium 30
Rendah
2 20
20
2 1
1 1 1
10
0
0
0
Tinggi
0 Rendah
0 Rendah
Kasus Magnesium Silicon Carbon CU Ni Kasus < 0,040 > 0,060
Pejelasan NG Magnesium
Knowledge Magnesium berfungsi sebagai pelarut molten metal untuk
Kenapa membentuk keuletan dalam benda kerja
Magnesium Ada beberapa
bisa NG? Factor….
Faktor – faktor yang mempengaruhi Magnesium rendah :
1. Add. Material cairan (Sb, Lmc.. dsb..)
2. Pemanasan Berlebih (Superheating)
3. Penahanan cairan setelah Mg Treatment
Material
plat baja
Ladle
Taamoak
samping
Lokasi FC
Mg Tidak (Free)
Tertutupl
plat baja
Mg
Core Problem 1 :
Material Mg Treatment jatuh menyebar di ladle
Step 2 : Analisa Kondisi yang Ada
Penambahan Penuangan PIC : Irfan + Supri
TAPPING Delivery Ladle
Mg Treatment ke cetakan Tanggal : 2 – 5 Mei 2021
Cairan
Molten metal
Ladle
Magnesium
Lokasi
Free
Core Problem 2 :
Cairan awal jatuh di Lokasi Magnesium treatment
Step 2 : Analisa Kondisi yang Ada
Penambahan Penuangan PIC : Ekwan + Suwanto
TAPPING Delivery Ladle
Mg Treatment ke cetakan Tanggal : 3 ~ 7 mei 2021
14’51’’
Waktu
Delivery Over
> 60 detik
Strategi :
1. Proses Meeting Online (Via Ms. Teams)
2. Proses Meeting Online (Via Aplikasi Meeting Gressmen)
3. Proses Meeting Outdoor (15 Menit 2x Pertemuan)
Aktifitas Circle Leader
2. Meeting Via Aplikasi 3. Meeting Outdoor Dengan Protokol Kesehatan (Durasi 15’) 2x Pertemuan
Aplikasi Meeting
Meeting diruang
terbuka
Lokaasi Meeting :
• Café
• Gajebo
• Dan lapangan
5m
2 Instal
3 Instal Stopper 4 stopper
Re-layout area pengunci ladle
1
Instal sutter Mg Sliding gate saat
Delivery ladle saat tapping
Treatment pouring
Implamentasi Training Kaizen
Mr. Supri Kaizen 1 Kaizen 2 Kaizen 4
Kaizen 3
Ayo.. Semangat ..
Kamu jadi
leader ya..
di kaizen!!
2,2
menit
3,6
menit
Jarak Jatuhnya
Jarak Jatuhnya
material Mg
material Mg
Treatment 2 m
Treatment 4 m
4M
2M
Step 6 : Penanggulangan
BEFORE KAIZEN 3
Step 6 : Penanggulangan
AFTER KAIZEN 3
Step 6 : Penanggulangan
BEFORE KAIZEN 4
Step 6 : Penanggulangan
AFTER KAIZEN 4
Step 6 : Penanggulangan
PDCA 1
Instal Cover
Spatter Pouring
Step 6 : Penanggulangan
Inovasi
Improvement 1
Result :
Step 7 : Evaluasi Hasil
Kaizen 1
Kaizen 2
Kaizen 3
Kaizen 4
42
Step 7 : Evaluasi Hasil
S afety
Kualitas Graphit OK..
Waktu Proses Pouring
uality
TERJAMIN
Tidak ada proses Recycle die karna Kontribusi dari
roductivity NG Komposisi Magnesium Kaizen Zone melting & Pouring 5,1%
ost
Activitas Circle Leader
Video Kebersamaan
AVE SUMBU X
AVE SUMBU Y
AVE SUMBU X
AVE SUMBU Y
LEADERSHIP
LEADERSHIP
ZONE
ZONE
MULTISKILL
MULTISKILL
KOMUNIKASI
KOMUNIKASI
ASSESSMENT ASSESSMENT
TEAMWORK
TEAMWORK
MOTIVASI
MOTIVASI
7 TOOLS
7 TOOLS
MEETING
KAIZEN
MEETING
KAIZEN
SAFETY
8 STEP
SAFETY
8 STEP
MEMBER MEMBER
GRAVITY GRAVITY
SUWANTO( CL ) 4.0 5.0 5.0 5.0 5.0 4.8 A 5.0 5.0 5.0 5.0 5.0 5.0 SUWANTO( CL ) 4.0 5.0 5.0 5.0 5.0 4.8 A 5.0 5.0 5.0 5.0 5.0 5.0
M. TEGUH .T( TL ) 4.0 4.0 4.0 5.0 3.0 4.0 B 4.0 4.0 4.0 4.0 4.0 4.0 M. TEGUH .T ( TL ) 4.0 4.0 4.0 5.0 3.0 4.0 A 4.2 5.0 4.0 4.0 4.0 4.0
SUPRIYANTO( NTL) 4.0 4.0 4.0 5.0 1.0 3.6 B 4.0 4.0 4.0 4.0 4.0 4.0 SUPRIYANTO. ( NTL ) 4.0 4.0 4.0 5.0 3.0 4.0 A 4.2 5.0 4.0 4.0 4.0 4.0
A. BASIT 2.0 3.0 3.0 3.0 5.0 3.2 C 3.6 4.0 4.0 3.0 4.0 3.0 A. BASIT 3.0 3.0 3.0 3.0 5.0 3.4 B 3.8 5.0 4.0 3.0 4.0 3.0
SULISDIYANTO 2.0 3.0 3.0 3.0 3.0 2.8 C 2.6 1.0 3.0 3.0 3.0 3.0 SULISDIYANTO 3.0 3.0 3.0 3.0 3.0 3.0 B 3.2 4.0 3.0 3.0 3.0 3.0
EKWAN P. 2.0 3.0 3.0 3.0 3.0 2.8 C 2.2 1.0 3.0 2.0 2.0 3.0 EKWAN P. 3.0 3.0 3.0 3.0 3.0 3.0 B 2.8 4.0 3.0 2.0 2.0 3.0
IRFAN B. 1.0 2.0 2.0 2.0 1.0 1.6 D 2.0 1.0 3.0 2.0 1.0 3.0 IRFAN B. 3.0 2.0 2.0 2.0 3.0 2.4 C 2.8 4.0 3.0 2.0 2.0 3.0
FADIL 1.0 1.0 1.0 1.0 1.0 1.0 D 1.8 1.0 3.0 1.0 2.0 2.0 FADIL 3.0 2.0 2.0 2.0 3.0 2.4 C 2.4 3.0 3.0 2.0 2.0 2.0
AVE GROUP 2.5 3.1 3.1 3.4 2.8 3.0 3.2 2.6 3.6 3.0 2.6 3.4
Result : Level Assessment naik X : 3,4
AVE GROUP
dan Y : 3,6
3.4 3.3 3.3 3.5 3.5 3.4 3.6 4.4 3.6 3.1 3.3 3.4
68% Sumbu X
D C
A
Before
X=3,0
Before Y=3,2
100
64% E 50
B
After 0
72% Sumbu Y
D C
STEP 8. STANDARISASI
PT. TOYOTA MOTOR MFG
SIGNED
INDONESIA
PLANT 2 WELDING
PRODUCTION
STANDARISASI Mujiono Suwanto Suwanto Mislan Tb rahman Zaenal
1
Stoper ladle saat - Masuk ke lobang - Stoper tidak bengkok
tapping ladle - Engsel tidak macet
M. Teguh T
Instal Karakuri
- Shuter bisa - Shuter bisa digerakkan Supriyanto
2 Shuter Mg
memutar - Engsel tidak rusak
treatment
A Basit
- Ladle mentok
gawang Sulis
<100mm
Irfan
14
Menghilangkan 1. Urgent 1. 12 bulan 1. Defect 1. 100 juta 1. 25 %
1 2. Sedang 2. 9 bulan 2.Complaint 2. 50 juta 2. 50 %
Defect Terak (Zanza) 3. Sangat Urgent 3. 6 Bulan 3. Reject 3. 10 juta 3. 100 %
1. Urgent
Menurunkan 2. Sedang 1.12 bulan 1. Defect 1. 100 juta 1. 25 %
2 Defect 3. Sangat 2. 9 bulan 2. Complaint 2. 50 juta 2. 50 % 11
over cutting (coak) Urgent 3. 6 Bulan 3. Reject 3. 10 juta 3. 100 %
1. Urgent
2. Sedang 1.12 bulan 1. Defect 1. 100 juta 1. 25 %
Menurunkan
3 Pemakaian material melting
3. Sangat 2. 9 bulan 2. Complaint 2. 50 juta 2. 50 %
v 9
Urgent 3. 6 Bulan 3. Reject 3. 10 juta 3. 100 %
THEMA :
Menghilangkan
Defect Terak (Zanza) di Line Melting
48
49