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Articulo 3-SMED

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45 views12 pages

Articulo 3-SMED

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Renzo Lozano
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© © All Rights Reserved
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INTERNATIONAL JOURNAL OF AUTOMOTIVE AND MECHANICAL ENGINEERING (IJAME)

ISSN: 2229-8649 e-ISSN: 2180-1606


VOL. 18, ISSUE 3, 8895 – 8906
DOI: https://doi.org/10.15282/ijame.18.3.2021.05.0682

ORIGINAL ARTICLE

SMED Simulation in Optimising the Operating Output of Tandem Press Line in the
Automotive Industry using WITNESS Software
A.Q. Basri 1, N. Mohamed1,*, Nelfiyanti1,2 and Yusoof Y1
1College of Engineering, Universiti Malaysia Pahang, 26600 Pahang, Malaysia
2Department of Industrial Engineering, Faculty of Engineering, Universitas Muhammadiyah Jakarta, 10510 Jakarta, Indonesia

ARTICLE HISTORY
ABSTRACT – The automotive industry is one of the most advanced industries in the world. The Received: 3rd May 2021
demand for vehicles keeps increasing over time, mainly influenced by technology’s sophistication Revised: 21st July
and impressive designs. This research is focusing on the production performance of the stamping Accepted: 12th Sept 2021
process in Malaysia’s automotive industry. The main issue observed and evidenced in data
collected from industry players is that an unacceptably long time is taken in the die/tooling change KEYWORDS
process, which grossly affects the planned production output. The most significant direct impact on Automotive industry;
this situation is the increase in operating costs due to additional time taken to meet the planned Dies changeover;
production output. Therefore, this research aims to establish a new framework that can optimise SMED;
WITNESS
the efficiency of the dies changeover process, which could lower the overall production cost, which
could partially transfer the saving to the consumers. The study was conducted in two stages; the
first is on data collection correlates with the automotive stamping premise to create a simulation
procedure, and the second is to analyse the current production output using WITNESS simulation.
These simulated output data have later been compared to the actual industrial data. Using a
systematic dies changeover process, a new alternative framework was proposed. The framework
combined single minute exchange of die (SMED), lean tools and simulation to become an
integrated single minute exchange of die (ISMED). It shows that the proposed method decreased
the changeovers processes from the initial of 1509.5 seconds to 750.75 seconds, then further
reduced to 569.75 seconds, with the nett time reduction of 62.2%. The result shows that the daily
production output has increased gradually from 1100 pieces to 1500 pieces, further increasing to
2145 pieces. As evidenced in analytical data, it is believed that this new framework can strengthen
the total output in the manufacturing process, especially in the manufacturing of automotive
stamping parts.

INTRODUCTION
The automobile industry is one of the most fascinating and well-known in the world. Since the introduction of
domestically produced automobiles in the early 1970s, the industry has attracted a lot of attention, had a big impact, and
experienced phenomenal growth in Malaysia [1]. Many parties are similarly impressed by its expansion, which has
attracted a diverse range of well-known businesses from around the world, all of which are vying for market share and
after-sales maintenance services [2]. Vehicle makers have produced a wide range of models in order to capture the
attention of customers and win their hearts. The automobile manufacturers’ marketing teams have examined and analysed
databases from servers to discover the best items for each market. As a result, potential purchasers have a wide range of
models to choose from to meet their diverse requirements.
According to the principle, a large lot size should be adopted in order to lower the cost of installing and upgrading the
equipment that runs through the set-up as much as possible [3]. Although traditional methods are used to reduce inventory
by producing a large batch, this strategy also contributes to excess inventory by producing more than what is required to
meet consumer demand. The theory of mass production is now widely acknowledged to be outmoded [4]. For mass-
production manufacturers, the key challenge was to retain price competitiveness and production efficiency. As a result,
it has become one of the primary motivations for automakers to focus on price, product quality, product differentiation,
and delivery performance at the same time [5]. To support modern manufacturing systems, producers must aim to create
a series of processes that allow them to focus on creating value while removing any distractions that slow down output
[6].
It is common to detect when the installation of machinery in the production cell in which the provision or exchange
of the equipment is an essential milestone towards meeting customer delivery criteria in organisations that utilise a
contemporary manufacturing lean production system [7]. Customers with a wide range of needs and low numbers require
organisations to make process enhancements that align production capabilities with customer expectations [8]. The time
it takes to make the changeover usually determines a producer’s ability to meet client delivery deadlines. In general, if
the exchange took a lengthy period, a higher group size is required [9]. Another problem for modern manufacturing is
meeting the increased demand for a wider range of products or made-to-order items. Product diversification entails the

*CORRESPONDING AUTHOR | N. Mohamed |  [email protected] 8895


© The Authors 2021. Published by Penerbit UMP. This is an open access article under the CC BY license.
A.Q. Basri et al.│ International Journal of Automotive and Mechanical Engineering │ Vol. 18, Issue 3 (2021)

production of a variety of commodities in lesser amounts, with the goal of maintaining total productivity [10]. The modern
manufacturing trend has seen a growth in product diversity as well as more frequent and smaller product orders. To match
this need, businesses must be able to create minor profits and provide new product models on a regular basis [11]. To
compete, businesses must identify ways to cut preparation and transition time by eliminating waste and ineffective
preparatory operations and converting conversion time into production time [12]. As previously said, the key problem
facing the production’s turn is to keep it as short as feasible. Single minute exchange of dies (SMED) saves time spent
setting up during operation.
SMED is a very popular method that can be used in optimising process time in die changes [13]. SMED is also an
important instrument to reduce lot size and provide a faster way to achieve maximum efficiency, which is one of the tools
of the lean manufacturing system (LMS) [14]. In an ideal world, the manufacturer could prepare each section separately
[15]. Simulation is needed to find out the results of the SMED application for further improvement. SMED itself is a
methodology used in reducing delivery time, economical production in small batches in responding to market demand
quickly [16]. Therefore, the purpose of this study is to reduce the set-up time at the stamping press line operation faced
by the automotive manufacturers. The study focused on the 1000 tonnage tandem press line where most of the medium
automotive body parts are produced. This study is very important as the manufacturers need to satisfy the customers’
demands within the promised time. It is continuous problems faced by the stamping line on how to reduce the total
production hours in completing the targeted production volume. Hence, the SMED methodology was used as a guiding
tool to analyse all the activities related to the overall stamping production preparation time in this study.

METHODOLOGY
A thorough explanation of how the study was conducted is presented, including the industrial problem identification,
data collection, working condition analysis, and the improvement of the current problem. This study focuses on the
application of Shingo’s SMED methodology to reduce non-value-added activities and to reduce the time required to
perform changeovers on various dies set/parts number or parts names at automotive stamping operation. Figure 1 shows
the research methodology flowchart, which consists of studying the problems associated with procedures in the tandem
press line, starting with identifying the main problems on the current die changeover activities, followed by the formation
of the ISMED framework and analysis involved during the study.
The data is collected using a series of monitoring procedures based on the SMED method. Observations of time gaps
and labour dispersion were also made and focused on during the study. Further, the implications of changeovers time on
the operation were implemented through software simulation. The WITNESS software used was to provide a clear picture
of the output based on the existing changeovers data. Hence, the critical issues were identified during the changeover
processes.

Start

Identify problem on current die change activity

ISMED framework

NO

WITNESS Model
Refinement

YES

Analysis and conclusion

End

Figure 1. Flowchart of research methodology.


Identification of Problem on Current Die Change Activity
Production in the stamping operation is very closely associated with the time available during the daily production.
The capacity of the press machine is determined on the basis of certain factors such as set-up time, downtime
(machine/operation/quality issues) and rest time. Therefore, it is very important to minimise the set-up time, which
contributes to the production efficiency during the operation hours. Operational planning has reliable data and monitors
the conditions of this stock on a regular basis. Therefore, to maintain a good safety buffer stock and ensure no short supply
of parts, the minimum buffer stock of three days per part is imposed.

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Stamping operations hours are often used for daily scheduling. However, there are also constraints on getting a
minimum stock of three days per part if there are a high number of downtimes as well as high set-up times. In normal
daily production, eight different parts are scheduled to be produced at a particular line. Consequently, there are eight
changeover activities to cater for production requirements. During the observation on the manner in which the changeover
activities were carried out in this circumstance, the daily operating production is inadequate to meet the production
demand. The main contributing factor was due to the high set-up time used during the changeovers process. Accordingly,
daily operations were extended to an additional two hours of working time. The direct impact of this situation is the cost
of production will increase, as well as prolonged the parts delivery and fatigued workers.
Therefore, the changeover activity needs to be improved at each job or task by identifying the non-value-added
activities involved. Thus, a comprehensive analysis focused on multiple lean manufacturing tools, significantly impacts
the whole production process. Appropriate lean manufacturing tools such as SMED, VSM, Kaizen, and job
standardisation can be used to solve the issues. In addition, there are also some effective analytical methods to solve the
non-value-added practices, such as Why’s analysis and Fish Bone analysis. However, with existing advanced technology,
varieties of simulations software are available to mimic the production processes with detailed explanations. The
simulation processes are able to identify the problems and are capable of suggesting the solutions depending on the input
by the users.
ISMED Framework Alternative
ISMED framework is a technique for the arrangement of the changeover issues experienced in the press activity. Thus,
ISMED is the new technique to settle the changeover exercises at the stamping shop that focuses on lean manufacturing
principles and decision-making as a major foundation. The established ISMED framework is organised into three key
elements, as illustrated in Figure 2.
i. Plan: define a problems / a problems overview & analysis / enhancement programs / validation
ii. ISMED approach: apply VSM, PDCA / 5 Whys analysis tools / work station design / standardization / simulation
/ SMED.
iii. Implementation of ISMED framework:
• To establish Standard Working Procedure (die change over)
• To implement training program under new S.O.P
• To set up a benchmark press line
• To integrate management view of involvement
• To enchant production plan to increase the number of stroke/day
In this study, the next step after the overall changeover procedure has been defined is the root cause problem
identification. Two common root cause analysis methods have been applied namely, Value Stream Mapping (VSM) and
Five Why’s analysis. The aim of using these methods is to identify any possible root cause problems and their patterns
from two different perspectives. Figure 3 describes the VSM in the changeover procedure.
The VSM assessment shown in Figure 3 is divided into four sub-stations based on job/task of changeover actions.
Since four machines are required for this tandem processing line, therefore, four sets of equipment for the tandem process
are necessary to produce a part. In this VSM assessment, the series of changeover activities from the beginning of the
process until it reaches the final process were examined. The root cause identification is then carried out using the Five
Why’s analysis tool.
The Five Why’s analysis is another root cause analysis method applied in this study. This analysis is used to support
the VSM analysis presented in the previous section. This analysis is a sequential process of asking ‘why’ five times in a
belief that the actual root cause of the defined problem will appear after asking ‘why’ five times. However, this
description regarding Five Why’s analysis procedure is not always necessary, and it depends on how the analysis has
been arranged and managed. Meaning that, it is not a significant issue of how many ‘why’ is being asked, instead of the
pattern of answers from a sequence of asking ‘why’ towards identifying possible root causes contributing to the defined
problem.
Simulation Analysis
WITNESS simulation software is used to identify important processes and to verify actual output based on production
data [13]. The WITNESS is used to describe the situation in reducing the waiting time to achieve good performance in
terms of consumer satisfaction [17]. WITNESS model simulated the current configuration, including the processes
involved in the stamping operation line. All the information required was defined and recorded in accordance with the
stamping procedures. The initial results from the current simulation should indicate the effect of the changeover practice
currently on the overall line production. All sub-process time has been considered in the total cycle time measurement,
including the transfer mechanism of robot loader and human-oriented movement. In running the simulation, data on
production planning with normal operating hours were used with the main focus on the changeover impact on the
stamping operation. Then, this simulation also aims to determine the results if the ISMED framework was applied to the
changeover activities.

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PLAN INTEGRATED SMED APPROACH IMPLEMENTATION


i. VSM applies to initial data i. To establish Standard
collection. Working Procedure
Research conduct in the Automotive
ii. To observe critical area (die change over)
Industry ;
1200Tone Tandem Press Line [refinement need] ii. To implement
iii. Overview of potential Lean Tools Training Program
under new S.O.P
˗ Overview research P: Plan
area. A research overall 5’S iii. To set up a
case study set-up 5 Why analysis Benchmark Press Line
˗ Observation of the
actual process. base on objective; iv. To integrated
review 4 stages Management view of
Define a ˗ Establish a suitable discuss. involvement.
problems Check Sheet.
v. To enchantment of
˗ Schedule activity Production Plan to
changeover. increase the number of
˗ Start to collect actual stroke/days.
data.
˗ Apply the D: Do
Conversational SMED To implement a Work Station
Review & approach. case study Design
analysis ˗ Review the result & procedure (base on
finding a potential area critical thinking &
to improve. finding).
˗ Start to implement C: Check
INTEGRATED SMED To overview all Standardisation
APPROACH. data collection by
˗ Completed all sequence simulation advance
Enhancement targets. anticipate
activity judgments [used
˗ Next, apply a SMED WITNESS]
approach.
˗ Review the result &
finding
˗ Transfer input at S-2 & A: Action
S-3 into Witness To finalise a Simulation
[simulation software] to discussion finding
proven data collection & conclude as
Validation activity. refinement activity
˗ To compare both to objective of the
results & discuss a new case study.
finding.
Figure 2. ISMED framework model.

Figure 3. Value stream mapping implemented in changeover procedure.

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RESULTS AND DISCUSSION


SMED (Conventional) Approach Execution
The external and internal elements were needed to be recognised in the second stage of the SMED method of the
changeover process. Thus, Table 1 classified the steps of the 21 procedures of the changeover processes. Table 1 indicates
that external and internal assessments were almost balanced when the number of changeover sequences of work was
identified. However, the main influence on the efficiency of SMED implementation would be the time for every job
sequence. In the internal elements, observation of improvements should also be determined as non-value-added activities
done by workers who were unfamiliar with monitoring of the press line. This would lead to several issues such as high
cycle time processes and repeated unsuitable ergonomic factors. Overall, by classifying the external and internal
changeover procedures based on the SMED approach, the study can implicitly focus on external activities. Therefore, the
amount of time spent in the changeover operations was measured on the basis of job sequences that had not been
effectively eliminated.
Table 1. Changeover activity classification on external and internal elements.
Seq. Element (Steps of SMED) Ext. Int.
1 Last good part from previous production ⁄
2 Move previous part run to next operation ⁄
3 Bolster out from the press machine ⁄
4 Get hand tool and loosen (8) bolts ⁄
5 Aside tool and (4) bolts from lower plate ⁄
6 Raise press ⁄
7 To remove dies from bolster to die storage area ⁄
8 Cushion pin setting (base on each parts pin layout) ⁄
9 Waiting for the tamakake operator bring the dies ⁄
10 Place next dies on the bolster and die setting ⁄
11 Machine attachment setting (Vacuum cup). ⁄
12 Get and thread 4 bottom bolts, start threads. ⁄
13 Move control pedestal, move machine slide down to die balancing (slide adjustment) ⁄
14 Upper die; hand tighten (4) top bolts, get hand tool to tighten bolts ⁄
15 Re-install upper die, loose upper dies clamper for dies adjustment (upper and lower) ⁄
16 Attach airline - quick change coupler ⁄
17 Cycle press - validate set-up ⁄
18 Set floor mat and one complete cycle panel produce ⁄
19 Get part for quality checking ⁄
20 Run/aside first part from next run and complete process part quality check ⁄
21 Complete process. Ready to proceed ⁄

The third stage of the SMED method is to separate the external and internal work, focusing on the external work
element. In view of the fact that external work elements are activities that workers can do while machines are still in
operation and the SMED theory points out that workers need to be more proactive in implementing this changeover
procedure aimed at reducing the total reported time. This self-awareness has an indirect impact on the overall success of
the changeover. The changeovers were carried out by two workers only at a high-frequency period, and their performance
often affects the recorded time of the changeover process
In the fourth and fifth stages of SMED implementation, the internal activities need to be shifted to the external
activities. Also, all other activities need to be streamlined. Thus, a careful study was needed to fulfil these stages of
SMED, whereby as many as possible to shift the internal activities to external activities. During the study, the main focus
was to observe the changeover activities by workers performing work while the press machine was running. In the case
of an observation made by the authors, the recorded time of the work sequence is the same if it was noticed. Significantly,
by doing this analysis, the efficiency of work handling by workers can also be monitored while they are working. It was
discovered during the study, the workers had to wait long time for the job sequence to complete. The direct result would
be the complete elimination of idle time during this changeover process.
Table 2 summarises the implementation of the SMED approach for the C line press. The changeover of job sequences
(21 flow of procedure) was divided into four sub-stations to follow the actual changeover processes at the press line.
During the assessment, there were four major areas of work in which information on sub-stations was to be implemented
by workers involved. By applying the SMED approach, external and internal work distributions at the level of all sub-
stations need to be identified and separated. However, all working procedures for sub-station 2, were recognised as
internal activities. Meaning that the amount of time recorded can be removed because the work carried out on the situation
of the press machines were still in operation.

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Table 2. Summary of changeover time achievement


Changeover time
No Items
Time (s) Time (min)
1 Initial changeover 1,509.50 25.16
2 SMED approach 750.75 12.51
ISMED Framework Approach
Detail stamping changeover processes was conducted during the initial study that traced every step from the beginning
to the end of the processes. By implementing the VSM method, it had evaluated the existing circumstances with the main
focus to eliminate non-value-added steps. With detailed input, the VSM processes path was drawn and studied for possible
improvements. The VSM assessment was divided into four sub-stations based on 21 changeover actions as illustrated in
Figure 4. Since four machines are required for this tandem processing line, four sets of equipment for the tandem process
were necessary for each part. The results of the VSM assessment indicated that the measured time for sub-stations 1 and
2 took longer time compared with substations 3 and 4. The initial data implied that many areas were not being optimised
during changeover activities, and still many non-value-added tasks need thorough analysis in order to achieve more
practical and effective assessments.

Figure 4. VSM implementation in changeover procedure.


Based on the VSM audit, special attention needed to concentrate on sub-stations with high changeover time, as listed
in Table 3. It was identified that sequence no. 4, 7, 8, 11 and 14 were considerably problematic activities that needed to
be analysed to define the key factors responsible for problems. However, sub-stations 1 and 2 were the most critical as
they covered the first 12 steps of the changeover process. For sub-station 1, the time recorded was 553.5 seconds, while
sub-station 2 is 583 seconds. Sub-stations 3 and 4, were less critical as they recorded 252.25 and 120.75 seconds
respectively. The total recorded time by the VSM method was exactly the same as the recorded time during the initial
changeover initial study, which was 1509.50 seconds.
Once the VSM assessment indicated areas for improvements, the next step of the study was to identify the root cause
of the problems. The root cause identification was then carried out by using the five why’s analysis. This approach helped
to eliminate the symptomatic layers, which could create a problem-solving root causes justification. This approach also
helped to be established the sequence between one origin and another root cause item.
Table 3. List of high changeover time.
Sub-Station Seq. no. Machine process SMED step Time taken (s)
1 4 All Machine Get hand tool and loosen (8) bolts 174
2 7 All Machine To remove dies from bolster to die storage area. 187
2 8 OP10 Cushion pin setting (base on each part pin layout). 109
2 11 All Machine Machine attachment setting (vacuum cup). 132
Upper die ; hand tighten (4) top bolts, get hand
3 14 All Machine 85
tool to tighten bolts
Improvement Activities
It is very important to come up with a new framework for the changeover process at the stamping line. As discussed
earlier, five problematic areas had been identified and need to be improved in order to make the productivity of the line
at the maximum level. This section focused on the improvement activities to address the identified problems of high-time

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changeover procedure and non-value-added activities. Table 4 listed improvement activities with the intention of
optimising the activity appropriate for implementation.
Table 4. Improvement activities conducted according to analysis.
No Issues Improvement
1 Get hand tools and loosen (8) To design one stop-centre for hand tools storage area. The purpose is easier
bolts. for the operator to find and reach. It is also can monitor operator usage.
2 To remove dies from bolster to To design a convenient dies storage condition purposely, easier for the
die storage area. operator to find and reach it back.
3 Cushion pin setting (base on To simplify the method of accessing @ references on dies cushion pin
each parts pin layout). layout.
4 Machine attachment setting To design one stop-centre for vacuum cup storage area. The purpose is,
robot (vacuum cup). easier for the operator to find and reach. It is also can monitoring operator
usage.
5 Upper die; Hand tighten (4) top Need to fully study ergonomic issues worker-handling and require re-
bolts, get hand tool to tighten. designing the purpose of the bolt for automated functioning with cost
impact.

The ISMED resulted in a significant time reduction in the recorded data, as shown in Table 5. The time on the internal
activities was not calculated by the SMED approach as well as the ISMED because of the time used during the machine
in operation. Therefore, the time used during internal activities was instantly removed and only focused on external
activities. The time recorded in the external element was 569.75 seconds which is equivalent to 9.50 minutes. Table 5
describes the comparison between the initial changeover activity, the SMED approach and ISMED approach. When the
SMED approach was introduced, changeover time was reduced from 25.16 minutes to 12.51 minutes, which is 50.3% of
the time reduction. Then, once the ISMED framework was implemented, changeover time was further reduced from 12.51
minutes to 9.50 minutes, which is another 24% of time reduction. Hence, the total time reduction was from 25.16 minutes
to 9.50 minutes, which was significant, at 62.2 %. The effectiveness of the ISMED framework had been demonstrated by
the results discussed and achieved the objectives of this study.
Table 5. Summary of changeover time achievement.
Changeover
No Items
Time (s) Time (min)
1 Initial changeover 1509.50 25.16
2 SMED approach 750.75 12.51
3 ISMED approach 569.75 9.5
WITNESS Simulations on ISMED Framework
The purpose of the simulation model is to define any abnormalities in the press system in order to verify problems
encountered during the stamping process. This simulation model allows detailed study in order to find possible
bottlenecks on the system. The simulation model shown in Figure 6 reproduces in detail the stamping part process of
Figure 5. The process started from the blank material first inserted into the 1200T press machines, followed by three 500T
machines. These machines representing four different processes according to the dies attached to them. Total cycle time
is measured from the blank material insert to the first machine process until the fourth machine completes the finished
good parts. All aspects of the transfer mechanisms were included as a sub-job in the pressing process. The simulation
model in Figure 6 is in consideration of elements mentioned in Figure 5 with additional input of part production; lot size,
part no, part name, model, and cycle time as in Table 6.
Table 6. Production planning on press line based on demand.
Lot Size Part No Part Name Model Cycle Time
200 PW932211 Sill Rear Floor Side Inner LH aaa 10
200 PW932212 Sill Rear Floor Side Inner RH aaa 10
200 PW932751 Side Member Front Inner LH bbb 10
200 PW932680 Side Member Front Inner RH bbb 10
300 PW932258 Cross Member Dash Lower Inner Center. bbb 9.8
400 PW932129/30 Cross Member Front Floor Front LH/RH ccc 9.8
400 PW932237/8 Panel Rear Floor Side LH/RH ccc 9.8
400 PW932299/990 Support Front Side Member Rear Inner LH/RH ccc 10.3

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Figure 5. Stamping tandem press operation fundamentals design for WITNESS simulation.
Furthermore, Figure 6 is the simulation of layout design and machines statistics on the ISMED approach
implementation using the WITNESS software model. The eight parameter inputs at initial resulting eight outputs with
detail simulation shown in Figure 7; with all elements in process initial layout (OP10, OP20, OP30, OP40) and other
mentioned in the database.

Figure 6. Simulation layout design on ISMED approach implementation.


The shown analysis in Figure 7 and Figure 8 describes the interpretation of the machine statistics and labour skills
after the establishment of the ISMED set-up system. In the simulation, the average idle was 33.33 % (reduced by 6.8%
from the initial changeover process), while the busy worker was 71% on average, which increased 31.7 % from the initial
changeover process. This indicates that, in this situation, the rate of productivity of workers had increased and had been
satisfactory.

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Figure 7. Machines statistic on ISMED approach implementation.

Figure 8. Labour statistics on ISMED approach implementation.


Referring to Figure 9, the ISMED approach showed that the capacity level of this press line throughout normal
working hours successfully achieved all eight parts with 2145 pieces of parts as per production planning. Without the
implementation of the ISMED framework, the line had just been able to produce five parts within eight hours of
production time. They needed extra hours to complete the remaining parts. The ISMED has proven to have positive
impacts on stamping production changeover activities.
Simulation Analysis
In this case study, the usage of WITNESS simulation software required data inputs from changeover specification
activities such as production parts planning information, cycle time, parts description, lot size, and the number of direct
manpower requirements for the stamping process. The stamping operations where the study was done used planning data
of 8 hours/day with two hours spare time for overtime production. This also meant the manpower utilisation was one
team for every stamping press line. After considering the numerous downtime activities, the planned capacity at the
stamping press line was 2000 pieces as the total output target per day. These inputs or information were the key elements
required to project the output of the line situation as the result of the impact of the changeover activities.
Overall, the research had recorded a marked improvement in changeover activities time at the stamping shop
department. The study had managed to prove the impact on the planning operations, such as increased in output or
production yield in 8-hour working time. In Figure 9, the change activity of the previous section shows the change of
activity time from the initial condition to the result of the ISMED application. The previous section showed that the

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recorded changeover time activity was reduced from 1509.5 seconds to 750.75 seconds when the SMED approach was
implemented, which was 50.3% of time reduction. Furthermore, the new framework (ISMED) recorded a reading of
569.75 seconds resulting in a 24% reduction more. The nett overall result of the changeover time reduction was 62.2%,
impacted by ISMED implementation.

Figure 9. Output of production on SMED approach implementation.

1600 100.00%
100.00%
1400 90.00%
80.00%
1200 1509.5 70.00%
1000 60.00%
Time (s)

50.26%
800 50.00%
600 40.00%
750.75 24% 30.00%
400
20.00%
569.75
200 10.00%
0 0.00%
Initial Data SMED ISMED
Time Percentage reduction

Figure 9. Summary of changeover time recorded.


The validation stages using WITNESS simulation software was meant to study the relation of the changeover time
improvements to the actual production output as spelt out in the objective of the research. Based on the maximum target
output in eight hours of working time per day was 2000 pieces, equivalent to eight part numbers of production.

2500 9
8 8
Target : 2000
2000 7
6 2145
6
Qty/day

1500 5 5
Parts

4
1000 1500
1100 3
500 2
1
0 0
Initial Data SMED ISMED

Quantity Stroke Quantity Part production

Figure 10. Summary of output impact vs changeover time reduction.

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A.Q. Basri et al.│ International Journal of Automotive and Mechanical Engineering │ Vol. 18, Issue 3 (2021)

By referring to Figure 10, the first analysis of the initial changeover data was recorded as 1509.5 seconds, which only
can produce 1100 pieces/day as suggested by the WITNESS software. Meaning that only five part numbers were able to
be produced in a day, even though there should be eight part numbers in actual planning. The remaining parts had to be
produced during overtime works and to be continued on the following day. By implementing the SMED approach at the
changeover activity, the total time recorded was 750.75 seconds; and the impact on the production operations was an
increase in the output value to 1500 pieces/day. This is equivalent to six part numbers being produced in 8 hours of
working time. Subsequently, the WITNESS validation was utilised using the changeover data from ISMED framework,
which was 569.75 seconds. The WITNESS shows, there was an output increase of 645 pieces from the SMED approach.
Hence, the new recorded output of 2145 pieces was equivalent to eight part numbers in eight hours of working time.
Consequently, based on this simulation results, it was strongly recommended that the production planning team to plan
the daily operations at 2200 pieces/day of total output.

CONCLUSION
This study focused on improving the current changeover activities at the stamping production line. The study started
by observing the current practice and figure out what were the main problems which contributed to the line inefficiency.
The study utilised the lean tools and simulation analysis during the investigation and later the improvement processes.
The SMED methodology and simulations were used during the first stage of the improvement activities, which involved
both internal and external activities of the changeover process. In the second stage, SMED methodology integrated the
lean tools, five Why’s analysis, and WITNESS simulations to identify the root cause of the problems into a systematic
framework in order to reduce the set-up time. The new approach known as ISMED traced all the problems during the
changeover activities. Finally, the ISMED framework had shown significant improvement from the initial condition to
the latest recorded data. The overall nett result of the changeover time reduction was 62.2%, and parts produced increased
from five parts to eight parts, which increased 37.5 %. The ISMED framework has proven to be successful and is the
novelty of the study. The ISMED framework is workable to other industries, interfacing changeover problematic
performances.

ACKNOWLEDGEMENT
The authors would like to be obliged to Universiti Malaysia Pahang for providing financial assistance under project
no. RDU1803166.

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