Quality Circle Training Overview
Quality Circle Training Overview
To
Quality Circle Competition
Team - प्रगति
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❑ Company Profile :- Spark Minda ([Link])
➢ Company & Product over view
Over view
• Business started in 1982
• ISO 9001 :2015
• Greater Noida • IATF 16949 Certified
• Haridwar • Total employees= 975No’s
• Pithampur
North Zone
Main Product is wire Harness
• Pune: II
West Zone
• Pune: I
• Murbad
South Zone
• Pillaipakkam (Chennai)
• Mysore
• Hosur
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❑ Major customers of Spark Minda ([Link])
2 Wheelers segment
Major Customers of Minda Corp Ltd- Gnoida
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❑ Manufacturing Capabilities at Spark Minda ([Link])
State of the art Machines and Equipment's for Wiring Harness operations
Plan
3 Define the Problem
Actual
Plan
4 Analyze the Problem
Actual
Identification Of Plan
5 Potential Cause &
validation Actual
Plan
6 Root Cause Analysis
Actual
Plan
7 Data Analysis
Actual
Plan
8 Developing Solution
Actual
Plan
9 Foreseeing Resistance
Actual
Plan
10 Trial Implementation
Actual
Plan
11 Regular Implementation
Actual
Plan
12 Follow up & Reviews
Actual
NOTE:- There is delay in activity due to “Holi holiday” but we manage with in next time frame
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STEP 1. Identification of Problems
➢ Brain storming on current Problems / Voice of customer/ Voice of Business
▪ Understanding the Current Situation at End of Line rejection at semi auto machines.
Customer complain
440
440
435
435
432
Parts in No's
430
430 430 ▪ Understanding the
428
current PPM at EOL
425 ▪ Target is to “Reduce EOL
425
422
Rejection up to 50%”
▪ For Further stratification
420 of EOL defects is refer
next slide
415
410
July.22 Aug.22 Sep'22 Oct'22 Nov'22 Dec'22 Jan'23 Feb'23
Qty in No's 440 430 435 432 430 428 425 422
STEP 1. Identification of Problems
➢ Brain storming on current Problems / Voice of customer/ Voice of Business
▪ Understanding the Current Situation at End of Line rejection at semi auto machines.
QTY. Cumm % Pareto trend for EOL Data collection for last 3 months
98 100 100 100
96
95
450 92
90 90
86
400 82 80
76
350 70
69
62
▪ Terminal back out
300 60 contribute 50% of the total
250 Selected for defect as observed from
50 50
210
Analysis Pareto trend
200 40 ▪ Therefore Terminal back
out is selected for
150 30 analysis and
improvement
100 20
▪ Further stratification of
53 terminal back out on next
50 30 27 26
10
17 15 12 9 8 8
slides
5 2
0 0
Short wire cut copper out Heat Sealing Hst Ng High core Terminal Terminal Terminal Tapping Mouth Wrong wire Wire colour
molding NG Bend Lock Fold Damage Open Open NG
STEP 3. Define the Problem
➢ Defect Description & Information
▪ Defect Description & Information
Customer : NA
Part Name : Wire Harness
MCL Part No. : 471403001700
Customer Part No : 471403001700
Complaint reported : Short molding
Function name : Harness wire
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STEP 3. Define the Problem
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STEP 4. Analyze the problem Short molding material catch
Short mold
material received
Finish Goods
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STEP [Link] of Potential causes & validation
➢ Fish bone diagram
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5.1: Identification of Potential causes & validation
➢ 4M = Material
❑ Verification – 1:- Short Molding -Mold temperature Not set as per specification at Higher limit
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5.1: Identification of Potential causes & validation
➢ 4M = Material
❑ Verification –2:- Short Molding -Mold temperature Not set as per specification at lower limit
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5.1: Identification of Potential causes & validation
➢ 4M = Material
❑ Verification –3:- Short Molding - Bumping Not done properly
Result:- From simulation trial we came to know that if we do not perform Bumping then “Air bubbles” get trapped on top portion of cover but it
will not contribute in short moulding.
Existing Controls:-
1). Bumping done 03 times as per work instruction
2). Level 3 skilled manpower used for molding process Conclusion : Not a Significant Cause
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5.1: Identification of Potential causes & validation
➢ 4M = Material
❑ Verification –4:- Short Molding - M/c. Pressure Not set as per specification
Result:- From simulation trial we came to know that if we increase or decrease pressure ,”Only flashes thickness will vary”
Existing Controls:-
1). Pressure is Freeze/set during “first piece approval” & regular monitoring done by
Quality & production team Conclusion : Not a Significant Cause
2). Level 3 skilled manpower used for molding process
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5.1: Identification of Potential causes & validation
➢ 4M = Material
❑ Verification –5:- Short Molding - Loading weight Not set as per specification ( Loading weight More)
Flashes Increased
Existing Controls:-
1). Manual control & operator dependent
2). Level 3 skilled manpower used for molding process
Conclusion : Not a Significant Cause
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5.1: Identification of Potential causes & validation
➢ 4M = Material
❑ Verification –6:- Short Molding - Loading weight Not set as per specification ( Loading weight less)
Short molding
Existing Controls:-
1). Manual control & operator dependent
2). Level 3 skilled manpower used for molding process Conclusion : Significant Cause
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STEP 6 : Root Cause analysis
FINAL CONCLUSION :–
Reason 1 - Because Terminal Lock press in case Crimping anvil is not properly Grind by Applicator Maintenance Technician
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STEP 7: Data Analysis
➢ Detail description about exact issue further course of action
Explanation
During investigation we found that Terminal lock struck Terminal Lock press in case Crimping anvil is not properly
with Anvil applicator therefore terminal lock get press Grind
(New Applicator Anvil needs to be grind before used )
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STEP 8: Developing Solution
Actions taken:– MIS-F & Displayed on line Training & Awareness given to Operators.
MCL
Sr. No. location Containment Action Evidence Photo Quantity Result Judgement
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STEP 9. Foreseeing Resistance
Conclusion:-
▪ Applicator Breakdown/Preventive maintenance to be update with Check point for Applicator Crimping Anvil Grinding
▪ Grind Crimping anvil used to avoid the lock press
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STEP 10. Trial Implementation
4000
Note:-
After Anvil Modification parts 22000 No’s run on line and
found “Zero terminal lock press issues”
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STEP 11. Regular Implementation
Status - Done
New Applicator Anvil used after Grinding
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STEP 11. Regular Implementation
3. Control Plan updated for Back out issue Status - Done
4. FMEA revised for Back out issue Status - Done
■ Horizontal Deployment .
• There is Similar type of fuse box Terminal used for All model
• (AAE,K74,KZK etc)
■ Tools Used.
Brain storming Pareto Chart Flow chart Fish bone dig Why Why analysis
Bar chart
Slide-
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STEP 12. Follow Ups & Review
500
Month Wise Issues at In -house 50 % Reduction
460 458 450 442 440
450 430 435 432 430 428 425 422 No fuse box terminal
400 back out issue reported
350
Action Taken
Number of Cases
300
250
200
150
145
120
PERFECT RESULT
115
95
100
50
0
April.2 May.2 June.2
Mar.22 July.22 Aug.22 Sep'22 Oct'22 Nov'22 Dec'22 Jan'23 Feb'23 Mar'23 Apr'23 May'23 Jun'23
2 2 2
Final Output:-
No of Cases 460 458 450 442 440 430 435 432 430 428 425 422 145 120 115 95
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STEP 12. Follow Ups & Review
■ Benefits.
■ Q & A.
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